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Performance and Oil Displacement Experiment Evaluation of PF601 Profile Control and Displacement Agent

摘要


This paper analyzes the stability and oil displacement efficiency of the displacement control agent PF601 in different mineralization degree and temperature for 30 days, and the influence on the wettability of the core, and proves the economic feasibility of the flooding agent PF601. The results show that the temperature and salt resistance of the reservoir is good, the ultra-low interfacial tension is maintained in 30 days, the contact angle is obviously reduced, the permeability is smaller, the plugging effect is better, so as to improve the recovery rate of this kind of reservoir.

參考文獻


Li Yuxiang, Tang Xiaofen, Liu Shuangcheng. Development and application status of chemical water plugging and profile control agents in my country's oilfields[J]. Oilfield Chemistry, 1995, 12(1): 88-94.
Bai Baojun, Gu Shuren. Analysis of factors affecting the plugging performance of gel plugging agents[J]. Oil and Gas Recovery Technology, 1997, 4(2): 22-22.
Sun Wei, Yang Shengzhu. Water plugging mechanism experiment of polyacrylamide plugging agent [J]. Oil and Gas Geology, 2002, 023(004): 332-335.
Han Ming et al. Deep profile control technology for thick oil layers. March 1997.

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